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  • 中国标准连:ISSN1005-2895
  • 续出版物号: CN 33-1180/TH
  • 主管单位:轻工业杭州机电设计研究院有限公司
  • 主办单位:轻工业杭州机电设计研究院有限公司、中国轻工机械协会、中国轻工业机械总公司
  • 社  长:刘安江
  • 主  编:黄丽珍
  • 地  址:杭州市余杭区高教路970号西溪联合科技广场4-711
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郭文博, 刘泓滨, 车应田, 周文杰, 周东华.飞机支线架注塑成型缺陷分析和多目标优化[J].轻工机械,2019,37(5):77-83
飞机支线架注塑成型缺陷分析和多目标优化
Injection Molding Defect Analysis and Multi Objective Optimization of Aircraft Branch Frame
  
DOI:10.3969/j.issn.1005 2895.2019.05.015
中文关键词:  注塑成型  熔接痕  气泡  浇注系统  多目标优化  TOPSIS综合评价法
英文关键词:injection molding  weld line  bubble  gating system  multi objective optimization  TOPSIS comprehensive evaluation method
基金项目:
作者单位
郭文博, 刘泓滨, 车应田, 周文杰, 周东华 昆明理工大学 机电工程学院 云南 昆明650500 2.中国铁建高新装备股份有限公司 云南 昆明650500 
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中文摘要:
      课题组以飞机支线架注塑成型过程中的熔接痕和气泡为优化目标,通过浇口位置寻优和更改浇口形式,消除了塑件成型过程中在浇口附近产生的熔接痕和气泡缺陷,同时发现了熔接痕和气泡在塑件成型过程中位置和形状的一致性;将浇口直径、模具温度、熔体温度、注射时间、V/P转换体积和保压压力作为工艺参数进行正交试验。通过工艺参数寻优,对熔接痕和气泡缺陷进行多目标优化,发现浇口直径对熔接痕和气泡的影响度较大,并得到最佳工艺参数组合为:模具温度60 ℃,熔体温度245 ℃,注射时间5 s,V/P转换体积99%,保压压力245 MPa,浇口直径1 mm。同时发现熔接痕和气泡在受工艺参数影响方面具有一致性,证明了熔接痕和气泡在形成机理、成形位置和形状、受工艺参数影响度的一致性。最终结果是熔接痕长度减少了35.66%,气泡面积缩小了26.74%。浇注系统和工艺参数优化2方面因素,为今后对熔接痕和气泡缺陷研究,以及工程生产中消除熔接痕和气泡缺陷提供了参考。
英文摘要:
      Taking the weld marks and bubbles in the process of injection moulding of aircraft branch frame as the optimization objective, the weld marks and bubbles near the gate were eliminated by optimizing the gate position and changing the gate form. At the same time, the consistency of the position and shape of the weld marks and bubbles in the process of moulding was found. The orthogonal test was carried out with the process parameters of the gate diameter, mold temperature, melt temperature, injection time, V/P conversion volume and pressure holding. Through optimization of process parameters, multi objective optimization of weld marks and bubble defects was carried out. It was found that gate diameter had a great influence on weld marks and bubbles. The optimum combination of process parameters was obtained as follows: die temperature of 60 ℃, melt temperature of 245 ℃, injection time of 5 s, V/P conversion volume of 99%, holding pressure of 245 MPa, gate diameter of 1 mm. Meantime, the consistency of weld marks and bubbles affected by process parameters was found, which proved the consistency of weld mark and bubbles in formation mechanism, forming position and shape, and the degree of influence of process parameters. The final weld line length was optimized by 35.66% and the bubble area was optimized by 26.74%. The study on two influencing factors of gating system and process parameters optimization provides reference for future research on weld marks and bubble defects and eliminating weld marks and bubble defects in engineering production.
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